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Fires 1998 January 08, 1998 - Shell Offshore Inc.
Remarks: Operator responded to an alarm in the compressor building and found a fire in progress on the left bank air intake filter and carburetor. The engine had a backfire through the carburetor and caused the air filter to protrude, allowing raw fuel to escape and ignite. Damage was to the air filter and cover, and a new carburetor. The compressor was repaired and back on line at 1900 hrs. 09-Jan-1998 - SOCO Offshore, Inc.
Remarks: Static electricity ignited escaping condensate vapors from the surge tank. The level in the glycol/condensate separator was low, just above the LSL shutdown switch. A hole found in the reboiler insulation on the top of the reboiler shell may have allowed oxygen in the vessel while it was in a static condition. 09-Jan-1998 - Walter Oil & Gas Corporation
Remarks: The glycol reboiler apparently malfunctioned and shut down on burner safety low. The well remained on production for an extended period allowing the circulating cool glycol to become saturated with fluids. Glycol reboiler startup operations were extremely accelerated. The onsite platform operator apparently failed to monitor the glycol reboiler and regeneration process for a period sufficiently to ensure proper operation before leaving the platform. 13-Jan-1998 - Chevron U.S.A. Production Company
Remarks: Operator responded to an alarm in the compressor building, and found a fire in progress on the left bank air intake filter and carburetor. The engine had a back fire through the carburetor and caused the air filter to protrude allowing raw fuel to escape and ignite. Damage was to the air filter and cover, and a new carburetor. The compressor was repaired and back on line at 1900 hrs. 9-Jan 1998. 17-Jan-1998 - Vastar Resources, Inc.
Remarks: The probable cause of the accident was that the packing around the valve stem for the wing valve on Well A-5 leaked gas into the atmosphere. The hot slag created the ignition source to start the fire on Well A-5. 22-Jan-1998 - ORYX Energy Company
Remarks: Condensate accumulated in the deck drain and was ignited from a hot weld shot spark. The instrument technician was not aware of the small accumulation of condensate in the deck drain. 30-Jan-1998 - Chevron U.S.A. Production Company
Remarks: Conducting cutting torch operations, over an open grating above an unprotected acetylene bottle. They did not position the acetylene bottle in an area safe from falling slag and did not cover the acetylene bottle with a protective barrier, such as a wetted tarp. Pre-hot work planning was incomplete and did not take into consideration the possible effects of falling slag. 31-Jan-1998 - Union Oil Company of California
Remarks: This compressor had become a high-maintenance item, and metal fatigue in the rocker arm bolts may have occurred, resulting in the fire. The rocker arm or push rod caused a hole in the valve cover, allowing crankcase oil to escape through this hole onto the exhaust manifold. 01-Feb-1998 - Texaco Exploration and Production Inc.
Remarks: Trace of free-standing condensate was ignited with cutting and/or welding slag. Extinguished immediately. No injuries and no pollution. 02-Feb-1998 - ORYX Energy Company
Remarks: A small fire occurred when lightning struck the flare boom during a storm and it ignited. The small fire was immediately extinguished by platform personnel. There were no injuries or damage associated with this incident. 03-Feb-1998 - Total Minatome Corporation
Remarks: A contract welder was making a torch cut on an old deck penetration from the top deck. Hot cutting slag apparently fell onto a standard canvas tarp that had been placed over an electrical wiring cable tray, resulting in a small fire. 08-Feb-1998 - Forcenergy Inc
Remarks: A faulty fan blade assembly exposed hot exhaust surfaces from the generator's exhaust system. Hot exhaust was saturated with turbine oil and there was no equipment integrity inspection in place. 09-Feb-1998 - Union Oil Company of California
Remarks: Compressor vibration caused the fuel line to become disconnected and/or the fitting may have not been sufficiently tightened when last disconnected. 16-Feb-1998 - Walter Oil & Gas Corporation
Remarks: The lay barge Cherokee was under tow by the motor vessel Gulf Cajun. 1,800 feet of tow line was laid out between the Cherokee and the Gulf Cajun. Seas were 8 to 10 feet. Visibility was limited because of fog. The Gulf Cajun could not be seen from the Cherokee. While under tow, the Cherokee struck the northwest corner of the platform. A 6-inch diameter pipe approximately 25 feet in length broke off the barge after penetrating the dry and wet compartments of the oil storage tank. The oil spilling from the oil storage tank ignited. The platform safety system shut in the platform. All personnel (7) were in their quarters at the time of the collision. Some personnel were knocked to the floor of the quarters. The survival capsule was engulfed in flames, making an attempt to abandon the platform by capsule impossible. The helicopter pilot and one other person managed to board the helicopter and flew in inclement weather to another platform. All other personnel used the escape ladder to the lower production deck. The operator made his way to the departing 8-inch gas pipeline and closed the manual shutdown valve to prevent the pipeline from fueling the fire. Personnel made an attempt to fight the fire and were successful at extinguishing several small fires; however, they could not extinguish the oil spilling from the oil storage tank. One 1,500-lb dry chemical unit, two 150-lb units, and several 30-lb handheld units were exhausted in fighting the fire. Personnel went to the +10 level of the platform and waited for help to arrive. After approximately 2-1/2 hours, a Marathon Oil Company boat arrived and picked up the personnel. The Marathon vessel extinguished the fire, using its fire monitor. 19-Feb-1998 - Pennzoil Oil & Gas, Inc.
Remarks: Towels that had been used to clean up cooking oil were washed and dried at a high temperature. The retained heat, combustibility of the cooking oil, and a mix of vented air apparently ignited the towels. The fire was extinguished. 20-Feb-1998 - Vastar Resources, Inc.
Remarks: Located in the port aft corner of the engine room, the Alpha Laval model MMB 304S-11-60 fuel oil centrifuge drive belt broke. With no drive belt, the centrifuge feed pump, which is motor driven, continued to pump fuel through the centrifuge bowl and into the overflow sump. There was no float switch installed in the overflow sump to kill the supply pump and activate an audio/visual alarm. We may never be able to absolutely determine the ignition source for the fire, because of the extensive damage sustained. However, the No. 3 engine Amot valve regulating jacket water to the watermakers from the No. 3 engine is highly suspect, based on visual evidence that the area around this valve is "ground zero" for the fire. The Amot valve has an electric motor actuator automatically operated on the basis of water temperature with contractors enclosed in the plastic housing on the Amot valve. The contractors do generate a small spark when actuated. The combination of high heat in the bilge (approximately 175 degrees F) and the solid deck plating created an environment for fuel vapors to collect. The right air/fuel ratio and a spark from electrical equipment (again, probably an Amot electric actuator) started the fire. Once begun, secondary fuel sources from the engines themselves fed the fire until it was extinguished. 20-Feb-1998 - Exxon Company, U.S.A.
Remarks: Small fire on insulation inside an 8"x8" enclosure at the above facility. A short in the emergency lighting circuit caused a high amp load, melting insulation, and starting a small fire inside the enclosure; the fire was extinguished using a handheld fire extinguisher. There were no injuries associated with this fire and damages of less than $500 were limited to the enclosure. It was determined that a broken conduit box was the cause of the short in the emergency lighting circuit. MMS visited the facility on Feb. 23, 1998, and Exxon's incident report and root cause analysis were provided to MMS. 20-Feb-1998 - Vastar Resources, Inc.
Remarks: It is believed that some type of flammable fluid was discharged from the drilling rig during simultaneous operations. A change in wind direction caused rig fluids to be discharged onto the exhaust piping of the generator. 25-Feb-1998 - Exxon Company, U.S.A.
Remarks: A fire was caused on the exhaust manifold of the No. 1 pipeline pump, caused by a failure of the pump engine's exhaust manifold which allowed hot exhaust to heat the burn shield material and ignite unburned fuel gas contained in the exhaust. The engine was shut down and the fire extinguished using a hand held dry chemical fire extinguisher. Damages were limited to the pump engine. There were no injuries. 03-Mar-1998 - Marathon Oil Company
Remarks: A small fire occurred on the No. 12 cylinder of the No. 2 field generator near the control panel. The fire lasted 2 to 3 minutes and was extinguished using one 30-lb. dry chemical extinguisher. The TSH on the cylinder shut down the engine. It appears that the gas leaked from the gas jumper line to the cylinder. Ignition source unknown. 04-Mar-1998 - CNG Producing Company
Remarks: A 3/8 x 2 inch pipe nipple on the No. 2 generator diesel fuel system cracked, releasing diesel fuel onto the hot surfaces of the engine. Engine vibration over-torqued the pipe nipple during installation/repairs twisting. 09-Mar-1998 - Apache Corporation
Remarks: A small flame was observed coming from the flame arrester of the chem-electric heater treater. The cause of the fire has been determined to be a collapsed fire tube. The fire was extinguished immediately and there were no injuries or pollution. 09-Mar-1998 - Vastar Resources, Inc
Remarks: A small flash fire occurred during compressor checkout. A small exhaust line was not connected and gas escaped from this line. The gas was probably ignited when it came in contact with a 24-volt open electrical box that was near the open line. One fire extinguisher was used to put out the fire and no equipment or personnel were damaged or injured. The fire lasted about 5 seconds. 11-Mar-1998 - Stone Energy Corporation
Remarks: Welding slag was burning through polyflow tubing and contacting natural gas. The master panel was not covered with protective material. The panel door opened while the ignition source was in the area. 15-Mar-1998 - Enron Oil & Gas Company
Remarks: A 4-inch block of wood was used for brace on a compressor muffler. The wood caught fire. The fire was put out with a 30-lb extinguisher. 15-Mar-1998 - Oryx Energy Company
Remarks: Personnel on the subject platform placed some ashes from their barbecue pit into a trash bag, which started to smolder. They immediately extinguished the fire with water and a fire extinguisher. No injuries or damages occurred because of the fire. The ashes that were placed in the trash bag were from March 14, 1998, and were felt to be suitable for disposal. Oryx instructed their personnel mix all trashes and coals with water prior to disposing of them in order to prevent future fires such as this. 15-Mar-1998 - Enserch Exploration, Inc.
Remarks: Welding operations were in progress to increase the capacity of the drip pan below the rotary table by raising the lip on the existing drip pan. Welding slag ignited a rag, resulting in a small fire that caused minor damage to an out-of-service wiring harness. The fire was extinguished immediately and there were no injuries or pollution. 20-Mar-1998 - Union Pacific Resources Company
Remarks: Gas fumes contacted a flaming torch. The gas being used to operate a starter and the exhausted fumes were not piped to a safe area. 28-Mar-1998 - Pennzoil E&P Company
Remarks: The probable cause of the fire was that gas residue at the controller flashed when the sparks made contact. 03-Apr-1998 - Shell Offshore Inc.
Remarks: Sixteen (16) gauge wiring, one main motor contractor, and two 15 amp/600 vac heater fuses were burned when 480 volts were inadvertently back-fed through the 32-volt heater coil contact and wiring. The 480 volts hit the 32 volt when a motor starter was manually closed. There were no injuries or pollution. 05-Apr-1998 - Samedan Oil Corporation
Remarks: The drilling rig Rowan Alaska No.1 generator caught fire as a result of a winding failure. The fire was extinguished immediately. Estimated damage was $10,000. There were no injuries and no pollution. 24-Apr-1998 - Chevron U.S.A. Inc.
Remarks: A fire occurred during welding operations on the platform. Sparks from the welding activity ignited gas from a leaking packing gland. A welding crew noticed the fire and the fire watch extinguished the fire immediately. 24-Apr-1998 - Newfield Exploration Company
Remarks: A plugged stack arrestor caused a back draft, forcing the flame in the firing chamber out of the flame arrestor. A lock nut on the burner air adjusting wheel was loose and apparently the air intake wheel vibrated closed. This caused an improper mixing of air and fuel, thus producing soot that plugged the stack arrestor. 25-Apr-1998 - Mobil Oil E&P Southeast Inc.
Remarks: An internal fire in the generator exhaust occurred because of the failure of the Kenco oil float level controller. 26-Apr-1998 - Forcenergy Inc
Remarks: A small fire occurred on the exhaust of the No. 1 pipeline pump because of oil spraying from a small crack on a stainless steel line on the No. 2 pipeline pump. Heat from the exhaust ignited the oil-soaked insulation. The fire was extinguished immediately with one portable dry chemical extinguisher. Damage was approximately $210. There were no injuries or pollution. 26-Apr-1998 - Unocal Exploration Corporation
Remarks: Hot refined oil from the No. 4 engine base came in contact with surfaces on the No. 2 engine turbocharger and exhaust system, which were operating at temperatures that exceeded the flash point of the refined oil. 18-May-1998 - Newfield Exploration Company
Remarks: The fire came from a leaking control line. The slag created from the welding of the drive pipe on the drill deck fell to the production deck. There were no tarps in place to isolate the production deck, but the distance between the welding and the control line was greater than 35 feet. 19-May-1998 - Chevron U.S.A. Inc.
Remarks: The probable cause of the fire was the WEMCO's blanket gas migrating past worn-out bushings around a rotating shaft and this same gas igniting because of an electrical short. After the fire an investigation turned up multiple shorts in the wiring of the WEMCO unit. Signs of arcing were found on the Agitator No. 3 motor. When the SCADA electrician, operations supervisor and day gauger changed out a motor on the No. 2 Agitator, there was arcing in two different places. Sparks shot from the electrical tape on the wires that were taped together inside the junction box, which was open, and also from the top of the motor. A wire that was on the No. 2 Agitator motor was bare in spots and some strands were broken. All of this wire was inside the conduit. 21-May-1998 - Conoco Inc.
Remarks: An investigation revealed that the insulation blanket had been soaked with oil. The high temperature at the outer shell of the exhaust collector ignited the oil on the blanket. Upon further investigation, the source of the oil was determined to have come from a 3/8" stainless steel seal oil supply line. The stainless steel line is approximately 1-1/2" long with Parker tubing fittings on each end. The line had a slight bend in it and a crack was discovered in the area of the bend. During normal operation of the compressor this line maintains a pressure of approximately 1,300 psi. Compressor vibration, along with the stress the bend was exerting on the tubing line, may have caused the line to crack. 22-May-1998 - Mariner Energy, Inc.
Remarks: A tarp caught fire and burned some gauges as well as a horn. 30-May-1998 - Texaco Exploration and Production Inc.
Remarks: Holes in the exhaust system allowed direct heat and possibly some hydrocarbons to reach the insulation covering the exhaust. The contributing causes of the fire were the corrosive gases and particles being expelled in the exhaust as well as age and rust on the piping. These items created the holes in the exhaust system. 07-Jun-1998 - Chevron U.S.A. Inc.
Remarks: The cause of the fire was a clutch failure possibly because of magnetic pickups and sensors that did not allow the clutch to fully engage. This partial engagement caused excessive heat to build up because of slipping, causing the rubber and other material in the pneumatic clutch assembly to ignite and burn. 14-Jun-1998 - Chevron U.S.A. Inc.
Remarks: A trash basket on the lift boat, Gulf Island III, caught fire. Construction crew used water to extinguish the fire, which lasted 2 minutes and resulted in no damage. 14-Jun-1998 - Unocal Exploration Corporation
Remarks: Hydrogen gas accumulation in the mud-logging unit wall cavities and electrical installations because of a system leak or leaks, resulting in ignition from an electrical source in the unit. Inadequate written procedure for leak detection contributed to the resulting fire and explosion. There was no ambient air gas detection system installed in the unit, which would have detected a leak. There was no flow-sensing device that could have detected a leak and shut in the gas at the bottle. There was no flame failure shutoff device on the individual FID or THA instruments. Wall and ceiling panels had unsealed penetrations and the panel edges were not sealed airtight. All of this contributed to allowing permeation with the hydrogen gas. Electrical boxes became saturated with hydrogen gas because of open enclosures. The electrical classification was non-explosive, since the mud-logging unit was internally protected from an external contamination of a combustible atmosphere by a positive pressure purge system bringing clean air into the unit from a safe area. The positive air purge system did not protect against internal releases of combustible gases. The positive pressure air purge system contributed to the buildup of hydrogen gas in the areas of permeation and saturation by not allowing air flow to sweep the areas and dissipate the gas. The positive air purge system did not include a combustible gas detection system. The electrical installation within the mud-logging unit was not classified weatherproof or explosion-proof, because it was installed in a positively purged building. Because of this, electrical boxes were allowed to become saturated with hydrogen gas to the point where ignition was allowed to take place. Ignition of the hydrogen gas is believed to have occurred due to the making or breaking of an electrical contact or switch or because of a hot electrical connection. The full bottle of hydrogen gas that continued to flow into the mud-logging unit supported the continuing fire. 20-Jun-1998 - Conoco Inc.
Remarks: Pipeline Pump A ignited and caught on fire. The fire was extinguished with 30 lbs of dry chemical. The fire kept re-igniting and was cooled down with water. The cause was the failure of the Pipeline Pump A motor cooler, which was then replaced. 20-Jun-1998 - Conoco Inc.
Remarks: The slag and sparks were hotter than the maximum heat tolerance of the tarp. The exceptionally hot and dry weather conditions contributed to the ignition. In addition, the tarp was new and not watered down. It appears to have been windy because the sump and tarp were located 40 feet below and 20 feet away from the area where they were welding. 25-Jun-1998 - Callon Petroleum
Remarks: The oil turbocharger bearing lubrication line broke and leaked oil onto the exterior of the turbocharger and the oil ignited. Vibration of the compressor caused the lubrication line to break. 26-Jun-1998 - Norcen Explorer, Inc.
Remarks: The probable cause of the accident was the breakdown of the insulating compound used on the generator's armature. 27-Jun-1998 - Sonat Exploration GOM Inc.
Remarks: During heavy thunderstorms a diesel generator began surging. The operator went to start a gas generator and during the startup a flash fire occurred. This resulted in the operator receiving 1st degree burns. The probable cause of the accident was a design defect in the control circuit that would allow the starter transformer to remain engaged indefinitely if a current-sensing relay was not satisfied. A contributing cause of the accident was the wrong setting being used on a current-sensing relay. This relay was in place to keep the starter transformer engaged until the motor current fell below the relay setting. This relay was set below the normal current rate; thus, it never released the transformer. 27-Jun-1998 - Shell Offshore Inc.
Remarks: During heavy thunderstorms a diesel generator began surging. The operator went to start the gas generator, and during startup a flash fire occurred and caused 1st degree burns to the operator. 08-Jul-1998 - Texaco Exploration and Production Inc.
Remarks: During welding on a heliport, slag fell in back of the protective tarps and ignited gas escaping from a gas fuel line through a loose connection. The fire was extinguished by the fire watch. The fire was an 8-inch high flame and was put out with a 20-lb hand held unit. 10-Jul-1998 - Vastar Resources, Inc.
Remarks: Lightning struck the top of the dry oil tank and a fire ignited. The fire was quickly extinguished with a 150 lb. Ansul wheel unit. A subsequent investigation revealed a pressure/vacuum relief valve on top of the tank was leaking gas to the atmosphere. The valve was repaired. The company sent out a Safety Alert to equip all atmospheric vessels and tanks with a blanket gas system and make sure they are grounded. 11-Jul-1998 - Pennzoil E&P Company
Remarks: An upset in the heater treater caused a shutdown of the low-pressure system, which caused the compressor to backfire and shutdown. Excess fuel flame extending out of the compressor exhaust was extinguished immediately. There were no injuries, no pollution, and no damage to the compressor. 16-Jul-1998 - Murphy Exploration & Production Company
Remarks: The Kenco engine oil level controller apparently failed to close after automatically adding oil to the engine crankcase. As the level of oil increased in the crankcase, the PCV valve began pulling oil into the engine air intake. Since all of this excess oil could not be combusted in the cylinder, it flowed out into the exhaust piping, continued to absorb heat, and ignited. 18-Jul-1998 - Chevron U.S.A. Inc.
Remarks: Heat tape on the control valve overheated or electrically shorted, igniting the fire. Gas escaping from the utility gas scrubber provided a continuous fuel source. The bottom drain on the gas scrubber was not fully closed, allowing a small and continuos flow of gas to feed the fire. 20-Jul-1998 - Shell Offshore Inc.
Remarks: Insufficient torquing of the nuts on the flanges to ensure the seal ring is properly compressed. 20-Jul-1998 - Pioneer Natural Resources USA, Inc.
Remarks: A loose exhaust bypass valve breather mount caused a spark igniting the escaping gas. The bolt holes on the breather were wallowed out, probably due to time and vibration. 27-Jul-1998 - Pennzoil E&P Company
Remarks: A small building (paint locker) on the top deck containing paint and thinner caught fire from spontaneous combustion. The fire was extinguished immediately with one dry chemical unit. No major damage, no injuries, and no pollution. 31-Jul-1998 - Shell Offshore Inc.
Remarks: A pipeline pump PAX-6040-B lubrication oil seal failed, resulting in a loss of lubricating oil and excessive temperature due to friction, causing the fire. 04-Aug-1998 - Conoco Inc.
Remarks: During welding in the production area, a piece of hot slag fell on a 3/8-inch piece of vinyl tubing containing supply gas, causing a fire. The gas was shut off and the flame was extinguished with 30-lb Ansul unit. 16-Aug-1998 - Mariner Energy, Inc
Remarks: A generator burned up and the crew immediately extinguished the fire. No injuries and no other damage done. 17-Aug-1998 - Chevron U.S.A. Production Company
Remarks: A construction crew was in the process of cutting grating to install a 3" x 3" angle iron support for tubing trays. Burning slag apparently migrated to the IP separator PSV pilot vent, resulting in a small fire, although the operator had implemented the required precautions prior to initiating the hot work. The small flame was extinguished immediately by the fire watch with one 30-lb. dry chemical extinguisher. There were no injuries, no pollution, and no equipment damage. 17-Aug-1998 - Samedan Oil Corporation
Remarks: A minor fire occurred in the rig mud room. An Ensco roustabout observed smoke exiting the blower vent on the traction motor of the mud pump. The cause of the fire was a leak in the seal between the motor and drive train, which allowed oil to enter the motor case. The fire was extinguished immediately with one CO2 unit. There were no injuries and no pollution. Final report. 21-Aug-1998 - Shell Offshore Inc.
Remarks: A small fire on EMD No. 1 was caused by oil leaking from a damaged gasket on the exhaust piping. The heat from the exhaust ignited the oil. The motorman extinguished the fire with a fire extinguisher. 12-Sep-1998 - Newfield Exploration Company
Remarks: Oil leak on the lubricator line dripped oil onto the exhaust and it flashed. The fire lasted only a few minutes and damage was under $500. 24-Sep-1998 - Callon Petroleum Company
Remarks: Upon the start of a diesel-powered generator, a fire developed, which was extinguished using a 30-lb. dry chemical extinguisher. Damage was confined to the internal part of the generator. There was no other damage. 01-Oct-1998 - Mobil Exploration & Production SE, Inc.
Remarks: While work was being done on the cellar deck, smoke was observed coming out of a rental welding machine not in use. Workers lifted the side panel up and noticed the wiring harness on fire. A short in the wiring is suspected as being the cause of the fire. 10-Oct-1998 - Mobil E&P Southeast Inc.
Remarks: A fire was started by slag from a welding operation falling to a lower deck and igniting vapors exiting a tank vent. 10-Oct-1998 - Amerada Hess Corporation
Remarks: Filter material had been left on top of the solar generator. When the generator was started the temperature built up and ignited the filter material. The fire was extinguished immediately. Damage to the compressor was minor. There were no injuries or pollution reported. 22-Oct-1998 - Leviathan Gas Pipeline Company
Remarks: High winds. 23-Oct-1998 - Chevron U.S.A. Inc.
Remarks: A contract employee did not communicate his intentions or follow correct welding and burning procedures. He did not request a permit to work sheet from the on-site supervisor or sufficiently inspect the welding area to ensure that the area did not contain flammable material. 29-Oct-1998 - Conoco Inc.
Remarks: A small fire occurred on WD 96-R when hot slag from welding operations on the subcellar deck (+35 level) landed on and melted through the plastic cover on the Fisher 2100 Level Safety High switch on the sump caisson. The instrument gas venting from the switch was ignited, resulting in a small fire approximately 1/2" in height. 01-Nov-1998 - Chevron U.S.A. Inc.
Remarks: The fire was caused by a lack of prestartup procedure and occasional checks of the compressor components. A contributing factor was the lack of a prestartup procedure review between the operator and the mechanic. 13-Nov-1998 - Exxon Corporation
Remarks: Welding was being conducted on the Dolphin Platform deck at the +10 ft level. The welder cut into the 72" caisson under the Dolphin Platform, where gas had accumulated inside the caisson. A small fire started. It self-extinguished immediately. The operator will use a gas sniffer in the future. 15-Nov-1998 - Chevron U.S.A. Inc.
Remarks: The weather conditions during the repair required workers use a tarp. The fire resulted from their not removing the tarp from the compressor upon completion. 19-Nov-1998 - Conoco Inc.
Remarks: The female end of the compressor interconnect shaft failed under load at rated speed. The resulting imbalance caused the broken shaft to oscillate, striking the retractable tunnel which, in turn, struck the lube oil supply connection to the compressor, dislodging it and allowing turbine oil to spray into the building. The oil contacted the engine exhaust and ignited, resulting in an open fire. 30-Nov-1998 - Vastar Resources, Inc.
Remarks: A Solar Centaur engine exhaust collector caught on fire. An operator's representative was in the process of starting the engine when he observed a small flame on the engine. He shut the engine down and extinguished the fire with a 30-lb. chemical handheld unit. The operator is searching for different types of gasket and sealing material for future use. 03-Dec-1998 - Newfield Exploration Company
Remarks: Spraying of oil on a hot turbo caused a flash fire because of engine temperature. The fire was immediately extinguished. There were no injuries or pollution reported. Damage was estimated at under $100. 05-Dec-1998 - Newfield Exploration Company
Remarks: A waste oil tank from another platform in the area was brought onboard and was hoisted above the slop oil tank by the platform crane. The drain valve on the waste oil tank had a nipple with a ninety-degree elbow pointing down (20' approx.), which was stationed directly over the opening of the slop oil tank. The waste oil tank emptied into the slop oil tank, through the grated deck, and onto the roof of the generator building below. From the roof, it moved onto a short section of generator engine exhaust that was not insulated, which then flashed. An electrician working nearby saw the fire and notified the production operator, who then put the fire out. There were no injuries, no pollution, and no damages. 06-Dec-1998 - Tennessee Gas Pipeline Company
Remarks: A 30" gas pipeline from WD 61 to shore ruptured on 12/6/98 and subsequently caught fire. The rupture occurred 2.5 miles from shore (state waters). Tennessee Gas reported that divers investigated the ruptured pipe and found that the line was 80 feet apart. Cause of the incident is unknown. On 12/14/98, Tennessee Gas informed MMS that the 80-foot pipeline section could not be found. 09-Dec-1998 - Marathon Oil Company
Remarks: The probable cause of this incident was the loose connection on the line side of the feeder breaker for the glycol heater. This connection may have not been sufficiently tightened during installation. 12-Dec-1998 - Vastar Resources, Inc.
Remarks: There was a small fire at the base of the glycol reboiler. It was extinguished with water a few minutes after the fire was detected. The reflux coils in the reboiler had a leak that allowed condensate-rich glycol and gas into the reboiler. The still column had a leak also. The still column and the reflux coil were replaced, and a new reboiler unit was ordered. 16-Dec-1998 - Shell Offshore Inc.
Remarks: The probable cause of this fire was corrosion and subsequent vibration, which caused a fitting to become loose at the main power connection cable to the motor lug. This condition caused excessive heating of the electrical connection, melting the rubber insulation boot over the connection. 19-Dec-1998 - Vastar Resources, Inc.
Remarks: The lubricating oil bearing and lambryth seal failed on the exhaust end of the generator turbine, causing a fire. The platform operator was in the process of starting the generator when the incident occurred. The small fire was immediately extinguished with water by the platform operator and mechanic. No injuries, pollution, or damage were reported. 23-Dec-1998 - Union Pacific Resources Company
Remarks: Two Grasso personnel were in the process of returning satellite well No. 3 to production when a large cloud of gas was released and then ignited. The two Grasso personnel and one Tech-Air helicopter pilot and the helicopter were on the satellite during the incident. All three victims were recovered from the water and transported to a facility located on Eugene Island 120. The helicopter pilot and one Grasso employee were treated for injuries. Attempts to resuscitate the other Grasso employee were unsuccessful and he was pronounced dead from apparent drowning. A nearby motor vessel extinguished the fire on the structure. The helicopter was determined to be airworthy and flown off the structure. 26-Dec-1998 - Shell Offshore Inc.
Remarks: A steel fitting on top of a hydraulic pump failed, spraying hydraulic oil onto the turbocharger, causing the fire. It is believed a manufacturers defect may have caused the fitting to wear prematurely, causing leakage and the subsequent combustion. Gravity and the location of engine exhaust in relation to the hydraulic oil leak saturated the engine exhaust, which contributed to the combustion. 27-Dec-1998 - Newfield Exploration Company
Remarks: Newfield experienced a fire on the No. 2 compressor at WD 152-A. The source of the fire was a gas leak from a short tubing line run between the PSV and pilot for the PSV on the second stage of the No. 2 compressor. The ignition source is unknown. It was extinguished within 5 minutes. The platform cook injured the back of his hand when the lid of the life jacket box fell on his hand while he was mustering at the escape capsule.
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